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HOPPING UP A FIRST- GENERATION 265 V-8

Adding 58 HP to a 180HP Stocker

If you have been around Chevys for 40 or 50 years, think of this story as a sort of “reunion.” For oh-so-many of us, that’s just what it is, a good ol’ reunion with Chevy’s very first small-block V-8 engine. Tens of thousands of TheAutoBuilder readers had one, and many still do. 

When we heard about this stock 265 and what its plan of attack was, we thought you would enjoy following along and seeing the process up close. All the owner wanted was for it to be blueprinted. He wanted all the horsepower and torque it could produce, but it still had to both idle and look like it was stock. The man to do the blueprinting was none other than renowned engine builder Joe Sherman.  

THE BLUEPRINT

Sherman knew full well that the original 8.0:1-compression ratio left a lot to be desired. He knew it could be measurably raised while allowing the engine to operate on pump gas. Problem: 265 domed pistons are impossible to find. The cylinders had previously been bored out 0.040 inch and there was no apparent wear, so Sherman thought the 0.040-inch oversize flattop pistons would work out fine. He did replace the rings, as well as clean the carbon off the top of each piston. 

To have an 8.0:1-compression with a flattop piston in a 265 means the cylinder decks are on the “thick” side. Sherman’s dial indicator dictated that the piston tops were 0.050 inch below the deck. His plan was to mill the cylinder block decks down 0.030 inch, leaving a new deck height of 0.020 inch.

The pistons are 0.040-inch oversize flattops in standard height. With block and head milling, the compression ratio was brought up to 9.6:1 from the factory original 8.0:1.

The original Power Pack heads had 58cc combustion chambers. Sherman got out his calculator and figured out that if they were milled 0.040 inch, they would be reduced to 53 cc. He then calculated both machining numbers and determined that with 4.0-inch bore sandwich head gaskets, the 8.0:1-compression ratio will now be 9.3:1. We were quietly thinking that this blueprinting alone might be worth 20 to 25 more horsepower in the little mighty mouse engine.

ooth and angular, Sherman pocket-ported the heads to measurably increase their flow characteristics. We thought that this would be worth another 15 to 20 hp.

COMP CAMS TORQUE CAMSHAFT

The ’55-’57 265 factory camshaft has a slot in its rear journal so the 1-3-5-7 rocker arms receive oil. Unfortunately, replacement camshafts have not had this slot for probably 40 years. No problem. In 1967, we used a grinder and rat-tail file to create a 2-inch-long groove that was 1/4-inch deep in the rear journal of our new cam. It worked fine. Consult your camshaft manufacturer or machine shop for a recommendation if you plan to update cams in your 265. 

Joe Sherman gave the valve pockets a three-angle valve job for a little better breathing potential. After this photo was taken, he sneakily pocket-ported each port under the valve and around the valve guide area to increase flow. This was good for 15 hp to 20 hp and more fuel economy at steady-state driving.

Sherman inspected the cam in this 265, then proceeded to create a similar notch in the chosen replacement, a Comp Cams hydraulic lifter (grind number XE250H-10, PN 12-230-2). It has a 0.432-inch intake valve lift and a 0.444-inch exhaust valve lift. The duration is 250 degrees on the intake valves and 260 degrees on the exhaust valves. The lobe separation angle is 110 degrees. 

From years of gas mileage testing and torque motor building in the ’70s and ’80s, we concluded that a valve lift of less than 0.450-inch lift would not adversely effect fuel consumption at part-throttle. We also felt that an advertised duration of 265 degrees or less would make the most torque over the longest and widest rpm range. This cam was right on. You don’t generally need to check for valve spring coil bind and piston-to-valve clearance until you get a cam with around 0.490-inch lift. 

ENGINE ASSEMBLY

All piston ring end gap clearances were checked, as was the crankshaft for rotational straightness. Factory-recommended clearances were adhered to throughout. The align bore of the main bearing webs was checked and was within spec. All of the engine’s bolts were then cleaned and inspected for thread rust, corrosion and stretch. The camshaft was degreed in at 2 degrees BTDC. (Note: Most camshafts are at 0 degrees TDC when installed, but when the timing chain stretches from use in 20,000 to 30,000 miles, the camshaft timing retards a few degrees. This takes away bottom-end throttle response and torque output, but gives it back at high rpm. The few horsepower gained back can be super-tuned into the engine, so we think advancing the camshaft 2 to 4 degrees in a street engine is a smart, must-do procedure.)

Again, to raise the compression ratio, 0.030 inch was milled off the deck, leaving a new deck height of 0.020 inch above the piston dome. Gas in 1955 did not have a lot of octane, so 8.0:1 was what the engineers thought the engine could live with. In short order, octane increased and so did compression ratios.

It goes without saying that the engine was assembled clean as a whistle. Because we assume you are a veteran reader and enthusiast, we do not wish to dwell on the engine assembly, unless it is something immensely beneficial. We do advise that you check oil pump pickup positioning with the bottom of the oil pan. This one was about +0.15 inch. In other words, the oil pan did not lie flat on the cork pan gasket. It could have been squeezed down by torquing the pan bolts, but oil seepage between the block and the gasket would have been the messy result. The pickup was repositioned and the pan made good contact with the cork gasket/block rails.

The reciprocating assembly was installed using factory-recommended clearances and torque specifications. Cleanliness is part of every Joe Sherman Racing engine package.

To our knowledge, Chevy head gaskets for a 3-7/8-inch cylinder bore have not been available for years. Luckily, a standard 4.0-inch bore gasket for a 350 V-8 works okay. The difference is 1/8 inch in bore size and no block coolant holes interfere. 

MALADJUSTED WCFB CARBURETOR

This 265 engine featured a nicely rebuilt Carter WCFB four-barrel carburetor, but on the initial start-up runs, the engine kept stalling after a few seconds. Sherman’s engine building and racing career commenced in the early-to-mid ’60s when Carter AFB and Holley carburetors were in vogue. He had no idea how to cure the ailing WCFB carb woes. He was about to call out the dogs for a replacement carb when we volunteered our services. 

“You know WCFB carbs?” he asked. 

“Ran ’em from 1961 through 1963. Used to rebuild ’em with our eyes shut,” we replied. 

“Have at it,” Sherman said, as he ventured into his office to answer an incoming telephone call.

Upon inspection, we immediately saw a flailing choke plate. It was not adjusted. Rather than rotate the choke housing, we simply loosened the locknut on the shaft and locked the plate in an open position. Few use a choke in Southern California. 

This is a Carter 0-2208 fuel pump. It produces about 5 psi of fuel pressure. Be advised that the WCFB carb’s needle and seat were engineered for about 5 psi, too. Some fuel pumps for Quadrajet carbs can pump out up to 9 psi. This will flood the cylinders, causing ring wear and hydro-lock. Be careful with what fuel pump you buy.

We also suspected that the accelerator pump was dry and was not pushing fuel into the primaries every time the throttle was opened. We were half-right. After removing the metering rod/accelerator pump cover, we saw that the pump adjusting mechanism was maladjusted. The accelerator pump was only working 50 percent at best. We quickly adjusted it for a full shot, and then reinstalled the cover.

Both fixes took five minutes, tops. Sherman came back and saw yours truly sitting on his dyno chair. 

“Can’t fix it?” he asked. 

“Nope, she’s ready to go,” we replied. Sherman then primed the fuel system by turning on his electric pump. The ignition key was switched on and the 265 fired right up and stayed “lit.” 

THE DYNO TESTS

After some steady rpm run time to break in the camshaft, Sherman reduced the engine rpm to idle-speed and proceeded to check the timing. He then blipped the throttle and saw that the distributor advance was working properly, so he took his seat at the dyno controls, pressed a few buttons and pulled the throttle. A number of dyno runs were made and each was no more than 10 seconds in run time. All of the engine vitals, such as water temperature and oil pressure, held true. The total timing had been at 32 to 34 degrees. Each run had produced 230 maximum horsepower. 

When the 265 would only run for seconds, the first thing we checked was the float level and the condition of the bowls. Everything was perfect. We then knew the problem was a faulty or maladjusted accelerator pump.

Sherman then bumped the timing to 36 to 38 degrees total. A few more runs were made and total horsepower peaked at a fraction over 238 hp. This 180hp 265ci (bored out to 275) small block was pumping out 58 more horsepower than stock, yet it idled as smoothly as it did when brand new.  

We would estimate that 20 to 25 of the 58 horsepower was coaxed out of the engine due to Sherman’s blueprinting. Another 15 hp to 20 hp was from the new Comp Cams camshaft (specifically, its higher valve lift). The rest came from the dyno headers. For the record, indexing the spark plugs and quickening the distributor advance curve would add a few more horsepower. We are sure the owner will address both areas.  

Where is this engine headed? Back into its three-on-the-tree, driven-on-weekends, header-equipped, semi-stock-looking classic. Only this time it will be many car lengths quicker and faster, and the steady-state fuel economy will be increased, too. 

The choke valve was flailing around, so instead of tightening the choke spring, we just repositioned the assembly nut on the shaft lock so the valve would be locked fully open. (No one we know uses a choke in Southern California). We also reshaped the accelerator pump rod so it would operate to the fullest. It was straight and let the pump work only about 40 percent, which was not enough to fuel the carb’s primary circuit.
To readjust the accelerator pump assembly, the top bolt above the pump must be loosened. Then the shaft can be positioned for best link-up with the exterior rod. Be sure to check the adjustment on the metering rods, too.
Here is a close-up of the best horsepower reading: 238.2 hp at 5,000 rpm.
The header primary pipes were too big in diameter, but Sherman thought
they would not hurt maximum power output, just mid-range. Block-decking,
head-milling and porting, plus a slightly bigger torque cam, equals 58 more
horsepower and a bunch more torque output (292 lb-ft at 3,400 rpm).

Article Sources


Joe Sherman Racing

714/542-0515

2302 W. 2nd St. Santa Ana, CA 92703

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